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Administrative - Formal · FY2010 · — · Final Order With Penalty · 2200000157

Penalty
Cost recovery
Compliance action

Case

Case Number
04-2010-5133
Type
Administrative - Formal
Lead
EPA
Outcome
Final Order With Penalty
Multimedia
Self-disclosure
N

Defendants (1)

Summary

7/27/10 - CONSENT AGMT ISSUED, ASSESSING A PENALTY OF $22,000, DUE NO LATER THAN 30 DAYS. ALLEGATIONS: ON FEB 2, 2006, A DRAIN VALVE AT THE TRUCK LOADING RACK WAS INADVERTENTLY HIT DURING EQUIPMENT MAINTENANCE. THE OPEN VALVE DISCHARGED INTO A DRAIN SYSTEM WHICH FLOWS INTO THE FACILITY'S OIL/WATER SEPARTOR. THE GASOLINE FLOW EXCEEDED THE CAPABILITY OF THE OIL/WATER SEPARATOR, WAS PUMPED THRU THE ACTIVATED CARBON CANISTER, AND ULTIMATELY DISCHARGED OUT OF OUTFALL 001. APPROX 5,387 GALLONS OF PREMIUM GASOLINE WERE DISCHARGED FROM THE FACILITY. IN RESPONSE TO THIS DISCHARGE, EPA CONDUCTED AN SPCC INSPECTION AT THE FACILITY ON FEB 4, 2006, IN ADDITION, EPA SENT RESPONDENT INFO REQUESTS PURSUANT TO SECTIONS 308 AND 311 OF THE CWA ON MARCH 3, 2006; JAN 22, 2008; JAN 27, 2008; AND JAN 21, 2009. RESPONDENT REPLIED TO EACH INFO REQUEST. BASED ON RESPONDENT'S ANSWERS AND THE INSPECTION, EPA DETERMINED THAT RESPONDENT FAILED TO IMPLEMENT ITS SPCC PLAN AS REQUIRED BY 40 CFR 112.3 IN ACCORDANCE WITH THE GUIDELINES FOR PLAN IMPLEMENTATION AT 40 CFR 112.7 AND 112.8. SPECIFICALLY, EPA ALLEGED THE FOLLOWING DEFICIENCIES: A. RESPONDENT FAILED TO KEEP THE MASTER FLOW AND DRAIN FLOW VALVE THAT PERMITTED DIRECT OUTWARD FLOW OF A TANK'S CONTENTS TO THE SURFACE ADEQUATELY SECURED IN A CLOSED POSITION WHEN IN A NON-OPERATING OR STANDBY STATUS AS REQUIRED BY 40 CFR 112.7(g)(2); B. RESPONDENT FAILED TO KEEP SUFFICIENT CONTAINMENT CAPACITY AT THE TRUCK RACK LOADING AREA AS REQUIRED BY

Source

Authoritative
EPA ECHO
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