# BADGER STATE ETHANOL, INC
> **Administrative - Formal** · FY2013 · — · —
## Case
- **Activity ID:** `3400119891`
- **Case Number:** 05-2013-5022
- **Type:** Administrative - Formal
- **Lead:** EPA
- **Outcome:** —
- **Penalty assessed:** —
- **Cost recovery:** —
- **Compliance action $:** —
- **Multimedia (multi-env):** —
## Defendants
- BADGER STATE ETHANOL, INC (complaint) (settlement)
## Summary

Badger owns and operates a fuel grade ethanol dry mill production facility at 820 West 17th Street, Monroe, Wisconsin (the Facility).The Facility includes two natural gas-fired dried distillers grains with soluble (DDGS) dryers (identified as Dryer A and Dryer B). Dryer AÂs emissions are controlled by a Regenerative Thermal Oxidizer followed by a Thermal Oxidizer followed by a Waste Heat Boiler. Dryer BÂs emissions are controlled by a Thermal Oxidizer followed by a Waste Heat Boiler.  All emissions exhaust to stack S10. On January 5, 2005, the WDNR issued Air Pollution Control Operation Permit No. #123038080-F01 (FESOP) to Badger for the Facility.  This FESOP expired on January 5, 2010.  Badger applied for a renewal on June 24, 2009, and FESOP No. 123038080-F01 is active as WDNR has not acted upon the renewal permit application.  Part I.A.5. of the FESOP Permit No. # 123038080-F01 prohibits Process P10 from emitting NOX  in excess of  0.10 pound per million BTU heat input.  On October 27, 2011, Badger submitted a quarterly CEMS report for July 1 through September 30, 2011. The  3rd quarter NOx emissions report submitted to EPA, showed that NOx emissions from Process P10 (Dryers A and B and the associated control equipment) were 0.113 lb per million BTU heat input based on the 30 day rolling averages from August 7 through September 8, 2011. 

Badger spent $196,600 for the root cause analysis and system upgrades to control NOx emissions.  Under the terms of the settlement i

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*Source: [EPA ECHO](https://echo.epa.gov/) · AI Analytics · CC0 1.0*